06/18/12 Started building location.
06/25/12 Blue Line Drilling moving on location rigging up.
06/26/12 Cemented 152′ of 8 5/8″ surface casing.
06/28/12 Total depth drilled 1,500′ at 8AM.
06/29/12 Total depth 2940′ at 8AM
06/30/12 Total depth 3962 at 8AM
07/01/12 Final T.D. 4525′ at 8 AM; Capps limestone 3996′-4010′ slight fluorescence, fair odor, fair oil cut; Gardner Limestone 4360′-4370′ slight scattered fluorescence, slight oil stain, trace odor; Gardner Sand 15 unit gas kick, good fluorescence, good oil stain, good to fair oil cut. Well logging scheduled for 6PM.
07/02/12 Cemented 4517′ of 4 1/2″ production casing using 500′ rubber coated casing from 1400′ to 1900′; second stage devation tool set at 2100′ pumped 250 sacks extended cement to cover the Coleman Junction.
07/16/12 Eagle Well Svc. scheduled to move on location next week.
07/23/12 Colman County Electric installed transformer; Eagle Well Svc. moving on location.
07/25/12 Eagle Well Svc. drilled out devation tool; Satterfield Wireline Svc. perforated the Bailey 1 from 4430′ to 4446′.
07/26/12 Standard Pump Svc. pumped 1000 gal. of 15% Hcl mud clean up acid; Eagle swabbed back; oil show on 4th swab run improving each run.
07/27/12 Shack Well Svc. fracked the Bailey 1 with 6100 lbs. sand
07/28/12 Started swabbing back 30% oil cut with fack flud at 11AM.
07/30/12 Ran tubing, rods, down hole pump, set pump jack, hooked up electricity, etc. Bailey 1 started pumping at 10PM.