12/14/13 Started digging pits and building location.
12/16/13 Blue Line Drilling scheduled to move on location Thursday
12/20/13 Set & cemented 170′ of 8 5/8″surface casing
12/22/13 Depth drilled 1,200′ at 9AM
12/23/13 Depth drilled 2325′ at 11AM conditioned hole and shut down for Christmas, will resume drilling Thursday.
12/26/13 Resumed drilling 2500′ at 6PM
12/28/13 Depth 4,136′ at 7:45AM; Gardner Lime 4362′-4368′ 20% fluorescence, 65 unit gas; Gardner Sand 4424′-4434′, 60-70% fluorescence, 124 unit gas, slow streaming oil cut, instant cut when crushed; TD 4548′ at 10 PM, logging well tomorrow.
12/29/13 Positive log analysis indicates Bailey 2 is stucturally high to all surrounding wells; 13% porosity; 13 Ohms resistivity.
12/30/13 Started running 5 1/2″ production casing.
01/15/14 Eagle Well Svc. scheduled to move on location Monday 01/20/14.
01/20/14 Eagle Well Svc. on location drilling out deviation tool.
01/21/14 Quail Wire Line Svc. perforated 4422′-4424′ gas flair on 4th swab run.
01/22/14 900′ fluid entry overnight gas flair with live oil; Standard Pump Svc. treated with 250 gal. 15% Hcl acid w/ clay stay & mud clean up additives started swabbing back.
01/23/14 Standard Pump Svc. fracked with 900 lbs. sand shut in well over night.
01/24/14 Started swabbing back frac water.
01/27/13 Running Rods, Pump, Tubing etc.
01/24/14 Started swabbing back frack fluid.
01/27/14 Ran rods, pump & tubing. Contacted Coleman County Electric.
01/31/13 Ran flow line waiting on Roustabouts to set Pump Jack, Tanks and Seperator.
02/27/13 Coleman County Electric installed transformer. Still waiting on Roustabouts
03/11/13 Roustabouts scheduled to start hooking up Pump Jack, Tanks and Seperator tomorrow.
03/12/14 Donica Roustabout Svc. starting to set up Pump Jack, Tanks, Seperator etc.
03/17/14 Donica Roustabout crew released due to incompetence. Calcote Dirt Contracting taking over equipment set up in the next couple days.
03/24/14 Bailey 2 equipment set up and started pumping