08/19/14 Started building location
09/02/14 Blue Line drilling scheduled to move in late next week.
09/10/14 Drilling rig delayed until next week.
09/16/14 Blue Line Drilling rigged up to start drilling. Cemented 160′ of 8 5/8″ surface casing, will resume drilling 10AM tomorrow.
09/17/14 Depth 440′ at 7PM.
09/18/14 Depth 1,100′ at 8AM
09/19/14 Depth 2,000′ at 8:26 AM
09/20/14 Depth 3,181′ at 4:55 PM
09/21/14 Top Palo Pinto Limestone 3,678′, 422 unit gas kick, 60% fluorescence, good odor, strong crush cut. Interval 3,696′-3,706 999 unit gas kick, 25-60% fluorescence, good odor at shaker, quick milky oil cut, strong crush cut. Top Capps Limestone 3,880′; 3,898′-3906′ 452 unit gas kick, 40-50% fluorescence, slow milky oil cut, fair crush cut. Depth 3,965′ at 4:15 PM.
09/22/14 Top Jennings Sandstone 4,166′, 723 unit gas kick, 10% flourescence, fair odor, slow milky oil cut, good crush cut. Gardner Limestone 4,300′, 660 unit gas kick, 5% fluorescence, good odor at shaker and in samples, slow milky oil cut, fair crush cut. Gardner Sandstone 4,362′, 709 unit gas kick, 20% flourescence, good odor, light milky oil cut, fair crush cut, all samples high gas with good odor. TD 4,467′ at 1 PM. Logging tomorrow.
09/23/14 Pioneer logged well, Palo Pinto Lime Stome 12% porosity 30 Ohms resistivity, Capps Lime Stone 7% porosity 30 Ohms resistivity, Jennings Sand Stone 14.5% porosity 7 Ohms resistivity, Gardner Lime Stone 9% porosity 32 Ohms resistivity, Gardner Sand Stone 7% porosity 65 Ohms restivity; casing crew ran 4,467′ of 5 1/2″ production casing; ordered Tanks.
10/23/14 Tanks delivered to well site.
10/24/14 Eagle Well Svc. moving on location next week.
10/28/14 Eagle Well Svc on location drilling out DV Tool. Coleman County Electric setting Electric poles.
10/29/14 Quail Well Svc. perforated 3696′-3,700′, Standard Punp Svc. treated well with 800 gal. 15% HCL, good oil cut by 4th swab run, improving on 5th swab. Shut-in over night.
10/30/14 Shut-in pressure at well head 300 psi. Opened valve, the well started blowing gas turned to pure oil after gas pressure subsided (less then 1 minute). Connected well to tank continued flowing oil into tank. Released the packer dumping KCL water down back side and the well continued flowing. Pumped 50 bbls. more KCL water to get well under control. Started running pump, rods and tubing.
11/03/14 Pump Jack hooked up, all equipment plumbed in, well turned on and in production.