09/06/13 Location staked rig scheduled to move in 09/22/13
09/21/13 Over 2″ of rain yesterday
09/23/13 Blue Line Drilling delayed due to the weather and rig repair.
09/24/13 Blue Line Drilling starting to move on location.
09/25/13 Waiting on parts to repair Crown Block
09/29/13 Started drilling & cemented 160′ of 8 5/8″ surface casing.
09/30/13 Resumed drilling at 5:45AM
10/01/13 Depth drilled 1,230′ at 10 AM
10/02/13 Depth drilled 1,590′ at 6 AM
10/03/13 Depth drilled 2300′ at 10 AM
10/04/13 Depth drilled 2800′ at 6 AM
10/05/13 Depth drilled 3,800′ at 10 AM
10/06/13 Depth drilled 4,167′ at 8 AM
10/07/13 Top Gardner Sand 4422′- 4436′ good oil fluorescence; good odor; good streaming oil cut. Lower Gardner sand 4448′- 4452′ light odor; slight oil cut. TD 4560′ logging well at 11 PM.
10/08/13 Logging completed 7:30 AM. Loggs indicate Gardner sand section 4,430′- 4,448′ with 15% porosity, 14 ohms resistivity, good Microlog. Started running 5 1/2″ production casing.
10/18/13 Eagle Well Svc. on location drilling out DV tool.
10/19/13 Quail Well Svc. perforated well from 4,430′- 4,448′
10/21/13 Standard Pump Svc. treated with 1,500 gal. 15% Hcl acid swabbed back.
10/22/13 Shack Well Svc. fracked well with 6,600 lbs. sand.
10/23/13 Started swabbing back frac water 800′ gas on each swab 15-20 min, left well open over night.
10/24/13 500′ fluid entry over night continued swabbing.
10/29/13 Poor fluid entry in well bore, did not recover 80% of acid water and frack water. The Gardner Sand formation absorbed a significant amount of drilling mud as indicated due to lost circulation when drilling. Loggs indicate reservior is not depleted, we will be refracking with nitrogen or Co2 to clean up drilling mud.
11/15/13 Nitrogen frac scheduled for Monday November 25, 2013
11/25/13 Frac rescheduled for next Tuesday due to weather
12/03/13 Basic Well Svc. Fracked well with 43,000# sand, 4495 scf nitrogen, 244 bbls water based gel. Started flowing back at 4:40 PM
12/04/13 Eagle Well Svc. swabbed the well dry, did not recover most of the frac water. No fluid entry slight amount of gas. pulled tubbing. Letting the well set will re-swab in a few weeks.
01/28/13 Eagle Well Svc ran tubbing back in hole first swab run hit fluid 100′ off bottom, no fluid entry the past several weeks. Evaluating potential use as an injection/disposal well.
07/28/14 Myers 1 approved as Salt Water Disposal well.