04/18/11 Eagle Well Service scheduled to move on location Thursday
04/20/11 T&T Well Service moved on location pulled the Velma Martin 3 replaced tubing and pump. Eagle Well Service delayed.
04/21/11 T & T pulled Velma Martin 2 replaced tubing and pump. Flow lines from Velma Martin 2 and 3 burst and are scheduled to be replaced.
04/22/11 T & T pulled injection well ran tubing and set packer, pressure tested to 500 psi. Released T & T rig, Eagle Well Service moved on location AA Martin 1.
04/25/11 Eagle Well Service cut paraffin and tested tubing on AA Martin 1
released rig to the Herman lease.
04/28/11 Eagle well Service moved back on location AA Martin 1. packer stuck in hole above Duffer zone; attempts to spear packer and fish out unsucessful; moved in reverse unit with mill shoe; started milling out packer.
04/29/11 Mill teeth on first shoe worn out; replaced mill shoe and resumed milling remainder of day. Roustabout crew replaced flow lines from Velma Martin 2 & 3 to tanks.
04/30/11 Second mill shoe worn out; replaced and resumed milling; retrieved top of packer, shut down for weekend.
05/02/11 Eagle Well Svc. continued to mill on packer half day due to severe weather.
05/03/11 Remainder of packer removed from AA Martin 1; started circulating to clean up hole; Velma Martin 2 & 3 flow lines tested and back pumping
05/04/11 AA Martin 1 cleaned out paraffin in tubing and pumped 1000 gal. 15% Hcl acid.
05/05/11 AA Martin 1 flowed back, started swabbed down and the well started producing oil and gas; ran rods, pump and tubing. Moved the rig to the Winn lease.
05/06/11 Winn 1 pumped 1000 gal 15 % Hcl acid; flowed back, started swabbing, good oil cut, good gas.
05/07/11 Winn 1 Basic Energy Svcs. ran 5000# 20/40 sand frac, shut in until Monday.
05/09/11 Winn 1 started swabbing back frac fluid; oil cut with gas on 4th swab run.
05/10/11 Winn 1 oil and gas cut increasing; circulated the well to flush out residual sand from frac job; ran tubing, pump and rods; waiting on Comanche County Electric to install new transformer.
05/11/11 Eagle Well Svc. moved to Winn 5 location rigged up then shut down at 11AM due to severe weather conditions.
05/13/11 Winn 5 cleaned out hole; pumped 1000 gal. 15% Hcl. acid swabbed back good oil cut with slight gas on swab runs. Ran tubing, pump and rods.
05/16/11 Moved to Winn 4 location encountered bridge plug above Duffer Limestone,drilled out bridge plug; started swabbing well.
05/17/11 Winn 4 pumped 1000 gal. 15% Hcl; acid job required substantially higher pressure then normal, Duffer Limestone does not appear to be open
05/18/11 Moved rig to AA Martin 2-C, pumped 1000 gal. 15% Hcl acid swabbed back 100′ pure oil each run; 15 min. per run.
05/19/11 AA Martin 2-C ran tubing, pump and rods reconnecting flow lines, started pumping; installed pump on Pitts injection well; moved rig to AA Martin 4-C Reverse Unit reamed out casing; pumped 1000 gal. 15% Hcl.
05/20/11 AA Martin 4-C started swabbing well shut down at 10AM due to severe weather.
05/21/11 AA Martin 4-C ran tubing, pump and rods.
05/23/11 AA Martin 2-A pulled, swabbed, ran tubing, pump and rods; moved rig to AA Martin 1-A pulled, swabbed ran tubing, pump and rods.
05/24/11 Velma Martin 1-A Basic Well Service pumped 600 gal. 15% Hcl flowed back and swabbed.
05/25/11 Velma Martin 1-A ran tubing, pump and rods.
06/27/11 Blue Line Drilling scheduled to move on Winn 1A location Friday July 1st
07/01/11 Blue Line moved on location rigged up and started drilling.
07/02/11 Winn 1A cemented 165′ 8 1/2″ surface casing; resumed drilling at 9PM.
07/03/11 Winn 1A drilled 1695′ total depth 1860′ at 9PM.
07/04/11 Winn 1A 2275′ at 8:30AM; Marble Falls 2514′ – 2546′, good florescence, good odor, good streaming oil cut, 30 units gas; Duffer 2712′ – 2722′, good florescence, strong odor, good streaming oil cut, 100+ units gas; top Ellenburger 2900′ very slight florescence, slight odor TD 3010′ at 11:37PM.
07/05/11 Pioneer Wireline Services logged the Winn 1A and 2912′ of 4 1/2″ production casing was cemented in place.
07/11/11 Eagle Well Service scheduled to move on Winn 1A location next week.
07/18/11 Eagle Well Service moved in on Winn 1A location; Satterfield Wire Line Svc. perforated Duffer interval 2706′-2724′ two shots per foot; Basic Well Svc. pumped 1200 gal. 15% Hcl and flushed with 1000 gal kcl water; color on 1st swab run, good oil cut on 2nd swab run increasing each run to 75% on 6th swab run.
07/19/11 Winn 1A ran tubing, pump and rods.
07/20/11 Winn 1A set pumping unit.
07/21/11 Winn 1A installed electric motor on pumping unit.
07/25/11 Winn 1A started production.
11/10/11 Perforated Winn 4 in the Marble Falls Limestone 2516′-2522′ and 2538′-2544′; pumped 1000 gal. 15% HCL acid started swabbing back.
11/11/11 First swab run 300′ oil and 100′ water in casing.